March 24th: Robotics Meeting
Today was OK.
In today's robotics meeting, unfortunately, it was discovered that one of our NEO Brushless motors are broken because the encoder connector had some cut up wires. We moved some motors around, and now our intake uses a regular CIM motor. We still need to test it though, but the electrical team is close to being finished with re-installing all of the motor controllers.
Hopefully the intake still works fine! Unfortunately, the programming team was unable to make any progress, but we were able to help around.
Thanks for reading,
Issac